hongyankevin
級(jí)別: *
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MR-J3驅(qū)動(dòng),QD75MH4定位模塊 控制X,Y,Z三根軸 X電機(jī)是3.5KW,Y,Z電機(jī)是2KW X,Y電機(jī)電纜接反,數(shù)據(jù)線接對(duì) 在不知情況下灌進(jìn)PLC和QP 開(kāi)始只有Z驅(qū)動(dòng)出現(xiàn)2032錯(cuò)誤,有時(shí)還有2033,2050錯(cuò)誤 后來(lái)Y,Z軸都出現(xiàn)2032錯(cuò)誤,怎么解決 |
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xyd_hsn10
jakenghuang
級(jí)別: 網(wǎng)絡(luò)英雄
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你是不是很高的計(jì)素,為何不用QD75P而用QD75M |
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syking1234
級(jí)別: 略有小成
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錯(cuò)誤2032 Error code 2032 Error name Overcurrent 1. Current that flew is higher than the permissible current of the servo amplifier. 1) Short occurred in servo motor power (U, V, W). 2) Transistor (IPM) of the servo amplifier faulty. 3) Ground fault occurred in servo motor power (U, V, W). 4) External noise caused the overcurrent detection circuit to mis-operate. Remedy 1. 1),3) remedy Correct the wiring. 1. 2) remedy Change the servo amplifier. 1. 4) remedy Take noise suppression measures. 既然知道錯(cuò)誤代碼,看QD75軟件里的幫助 |
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